beepa, here is an answer in part with perhaps more to follow...
F-35B starts critical tests in comeback attempt Stephen Trimble 05 Oct
2011
http://www.flightglobal.com/news/articl ... pt-362941/
“...The cracked bulkhead has been patched up and redesigned and three of the five glitches in the propulsion system are already permanently fixed. Of the remaining two issues, one fix is scheduled to be approved in December, and the last problem should be resolved in February 2012, Robling added. Although the F-35 was grounded for 16 days in August, the electrical system at the root of the problem is common to all three variants.
Meanwhile, programme officials also appear to have resolved a 90.7kg performance shortfall in the vertical lift bring-back weight of the F-35B in hover while returning to a ship. Engine manufacturer
Pratt & Whitney has confirmed the solution includes raising the output of the propulsion system by about 100lb-thrust (0.4kN)...."
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Pratt Advances On F135 Stovl Boost Plan – Apr 6, 2011 By Guy Norris
http://www.aviationweek.com/aw/generic/ ... line=Pratt Advances On F135 Stovl Boost Plan
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“Pratt & Whitney has updated progress on a four-point plan to help Lockheed Martin correct issues with the F-35B short take-off and vertical landing (Stovl) variant, development of which has been placed "on probation" by Pentagon leadership....
...Describing additional details of the company's four-point plan for the F135-600 Stovl engine variant, Boley says first "we have to understand what role we have in any additional vertical lift bring back (VLBB). We can provide more thrust if that's desired." The overall VLBB requirement, which refers to returning for a vertical landing with an unused weapons load corresponding to two 1,000-lb. JDAMs and two Amraams, is around 3,000 lb.
Lockheed Martin "is not asking for more thrust, but if we did provide it, it will be 100 lb., which is easily accommodated," Boley says. The thrust delta, achieved through a scheduling change in the full authority digital engine control, is so small compared to the engine's overall max hover thrust capability that it could "almost be a production variability."
Thrust increase would necessarily have to be spread evenly throughout the system, which, in hover mode, diverts around 16,000 lb. through the engine's main nozzle, 20,000 lb. via the lift fan and an estimated 4,000 lb. through the roll posts. Pratt formerly indicated the main nozzle delivers 15,700 lb., the lift fan 20,000 lb. and roll posts some 3,700 lb., combining for a total of 39,400 lb. thrust. However, the company confirms total max hover thrust is now "greater" than 40,000 lb. In conventional up-and-away mode, the F135 is rated at 43,000 lb. thrust. Lockheed's "stack up" of items that will increase VLBB is mainly being tackled through further trimming of unspecified empty weight and other non-engine-related changes, Boley says...."
A4G Skyhawk: www.faaaa.asn.au/spazsinbad-a4g/ & www.youtube.com/channel/UCwqC_s6gcCVvG7NOge3qfAQ/videos?view_as=subscriber