| Date |
Status |
Local S/N |
FY/n |
AF/Unit |
Version |
Info |
Details |
| 22 Nov 2005 |
[act] |
90824 |
90-0824 |
14 FS |
F-16C Block 50B |
|
Details
|
|
|
|
|
This aircraft made an emergency landing Ninoy Aquino Manila International AP, Philippines due to hydraulic problems. Aircraft was on a return leg from Cope India 05 and was not damaged. Volunteers had to be recruited to push the aircraft to it's parkings space on the ramp as the aircraft lost power after landing. A US Air Force C-130 aircraft arrived Thursday 08 Dec at the Ninoy Aquino International Airport (NAIA) Terminal 1 to deliver a new engine for the F-16. It was initially reported that the jet lost its hydraulics and emergency brakes en route to the Misawa Air Base in Japan. Inspection of the jet, piloted by Capt. Justin Dupuis, showed that its engine had to be replaced.
|
|
| 28 Nov 2005 |
[act] |
89133 |
89-2133 |
36 FS |
F-16C Block 40G |
|
Details
|
|
|
|
|
While landing in a severe cross wind, the jet departed the runway during landing roll at Osan AB, Korea. Right main landing gear collapsed and was ripped off the aircraft leaving a hole in bulkhead 341 where the strut mounts the clevis. Much more damage was done to the entire airframe. When the engine was removed, pry bars were used to open the CSD door because the standby generator and the system pump had been crushed together. Although a class-A mishap, the aircraft was still repaired and returned to the 36th FS.
|
|
| Unknown |
[i/a] |
88404 |
88-0404 |
93 FS |
F-16C Block 30K |
|
Details
|
|
|
|
|
Ran off the runway at Balad AB.
|
|
| 14 Mar 2006 |
[w/o] |
89099 |
89-2099 |
35 FS |
F-16C Block 40F |
News Article
|
Details
|
|
|
|
|
Lost at sea around 09:30 hours twenty miles off the coast of Kunsan AB, Korea. Pilot was Capt. Donald Siegmund, of the 35th Fighter Squadron ejected safely and returned to base shortly after. He spent about 55 minutes in the water before a South Korean air force rescue helicopter dispatched to the scene found and lifted him to safety.
|
|
| 30 Mar 2006 |
[w/o] |
89115 |
89-2115 |
421 FS |
F-16C Block 40G |
News Article
|
Details
|
|
|
|
|
The pilot, 1st Lt. Jay Bear, was conducting a close-air support training mission over the northern Utah Test and Training Range. He ejected safely. The aircraft went down in a muddy tidal area along one of the islands in the Great Salt Lake. The nature of the problem with the jet was not immediately know. It will likely take months to complete the investigation.
|
|
| 05 Apr 2006 |
[w/o] |
93542 |
93-0542 |
55 FS |
F-16C Block 50Q |
News Article
|
Details
|
|
|
|
|
At around 17:40 hours - while on a two ship training mission over the Atlantic, 30 miles off the coast of South Carolina - this F-16 went down. The other pilot in the flight saw the ejection and a parachute open but it was not untill 19:35 hours that the pilot, Captain Theodore 'Ted' Shultz, was rescued by the US Coast Guard. The cause of the crash was determined to be a G-LOC incidence.
|
|
| 11 Apr 2006 |
[w/o] |
83164 |
83-1164 |
62 FS |
F-16C Block 25B |
News Article
|
Details
|
|
|
|
|
The plane crashed at 09.55 hours local time. The pilot safely ejected right after flames were seen at the rear end of the jet. The F-16 went down in the Northwest Valley, in a farm field near Loop 303 and Indian School Road. The accident occured shortly after the jet took off from Luke AFB for a two-ship training mission. The pilot, 26-year-old Captain Jason Attaway, ejected safely. An explosion of the Pratt & Whitney engine was blamed for the crash.
|
|
| 26 May 2006 |
[act] |
84326 |
84-1326 |
302 FS |
F-16D Block 25D |
AIB Report
|
Details
|
|
|
|
|
Due to a oxygen mask disfunction, the second pilot was cut from oxygen during the climb-out. He suffered severe hypoxia and died by this cause.
|
|
| Sep 2006 |
[act] |
92455 |
92-0455 |
416 FLTS |
F-16B Block 15AR OCU |
|
Details
|
|
|
|
|
Right main gear wouldn't lock in the down position. After two hours spent working the problem pilot landed at Edwards AFB, California. The aircraft skidded down the runway with the right wing on the ground. Ultimately the aircraft stopped facing the opposite direction. Pilot was fine, no ejection was required. Exact date is unclear but was between the 10th and 16th of September. Will be repaired shortly.
|
|
| 14 Sep 2006 |
[w/o] |
91337 |
91-0337 |
22 FS |
F-16C Block 50B |
News Article
|
Details
|
|
|
|
|
The aircraft suffered a landing gear failure near Spangdahlem AB after hitting an antenna during a landing attempt. It ran out of fuel before the problem could be fixed and the pilot, 1st Lieutenant Trevor Merrell, executed a controlled bailout. The accident was caused by a visual illusion at Spangdahlem AB. The runway has an upslope, making the pilot think he is coming in too high, forcing him to take a lower approach, with all consequences.
|
|
| 21 Sep 2006 |
[act] |
94047 |
94-0047 |
77 FS |
F-16C Block 50 |
News article
|
Details
|
|
|
|
|
Suffered a fire in the exhaust during take off from Shaw AFB and the pilot jettisoned the tanks over civilian land. The aircraft landed safely and was repaired.
|
|
| 26 Oct 2006 |
[w/o] |
84296 |
84-1296 |
62 FS |
F-16C Block 25E |
News Article
|
Details
|
|
|
|
|
Experienced an engine fire during takeoff roll at Luke AFB, Arizona but aborted before lift off. Fire crews sprayed foam on the aircraft and the pilot was treated at the scene. Early reports said the pilot ejected, this turned out not to be the case as images from the scene show the canopy still in place. Early reports also incorrectly reported that the aircraft tookoff and returned to Luke AFB with an emergency landing. Excerpt from the crash report: "After being cleared for takeoff, Colonel Sherman taxied to the left side of the runway accompanied by Captain Cuadra on the right side. Upon ignition of the afterburner, Colonel Sherman heard an explosion and noticed that a fire had started on his aircraft. His wingman transmitted "Fire" on the radio and Colonel Sherman applied full brakes and initiated the appropriate critical action procedures to abort the takeoff due to fire and preparing to get out of the stopped, but burning aircraft. He was able to open the canopy and safely exit the F-16. Members of the Luke AFB fire department extinguished the aircraft fire". Cause was determined to be a failure of the 3rd stage when the disc fractured putting three holes in the airframe. The resulting fire burned the entire aft section of the aircraft.
|
|
| 17 Nov 2006 |
[act] |
91471 |
91-0471 |
13 FS |
F-16D Block 50D |
News Article
|
Details
|
|
|
|
|
Smoke filled the cockpit forcing the pilot to make an emergancy landing at Hakodate Airport at around 9:56 hours local. Pilot and aircraft are ok. The cause is still unknown.
|
|
| 27 Nov 2006 |
[w/o] |
90776 |
90-0776 |
524 FS |
F-16C Block 40K |
News Article
|
Details
|
|
|
|
|
Went down over Iraq north of Falluja in western Anbar province at 13:35 hours during a combat mission supporting ground forces. The official cause of the accident was "chanalized attention manifested by the pilots to maintain a constant visual positive identification of targeted enemy vehicles and subsequent target fixation on these vehicles while they were traveling at a high rate of speed". Unfortunately the pilot, Major Troy L. Gilbert of the 309th FS, was killed in this accident.
|
|
| Dec 2006 |
[act] |
89001 |
89-2001 |
555 FS |
F-16C Block 40E |
|
Details
|
|
|
|
|
Unknown details, was damaged in some form of mishap. Exact date also unknown but is around mid December 2006. Has been reported as a either an engine run accident or a landing accident. Mishap is still under investigation.
|
|