| Date |
Status |
Local S/N |
FY/n |
AF/Unit |
Version |
Info |
Details |
| 01 Jul 1994 |
[w/o] |
83173 |
83-1173 |
182 FS |
F-16B Block 15S |
|
Details
|
|
|
|
|
Crashed at about 10:20 hours some 100 mile from Kelly AFB, Texas, at the Crystal Military Operating Area. The incident was during a training mission. Both crew ejected safely and where treated for minor injuries.
|
|
| 20 Sep 1994 |
[w/o] |
88488 |
88-0488 |
421 FS |
F-16C Block 40C |
|
Details
|
|
|
|
|
Crashed at about 11:00 hours in a cornfield 12 miles away from Hill AFB, Utah. The aircraft was on a training mission on the Utah Test and Training Range. The pilot, Capt. Michael D. Goldfein, safely ejected and landed in the Great Salt Lake. He was rescued by a UH-1 from Hill’s 545th Test Group and released from hospital after examination. A faulty fan blade in the engine was the cause of the crash
|
|
| 25 Oct 1994 |
[w/o] |
90814 |
90-0814 |
4 FS |
F-16C Block 50B |
|
Details
|
|
|
|
|
Captain Rappa ejected safely near Wendover, Utah.
|
|
| Unknown |
[act] |
92887 |
92-3887 |
13 FS |
F-16C Block 50P |
|
Details
|
|
|
|
|
The aircraft made a landing on the runway at Misawa AB with no nose gear when the nose strut refused to extend on approach. The pilot landed it perfectly on the main gear and touched it down on the ECM pod. The pod saved the aircraft form exstensive frame damage and also saved the HTS pod from being wrecked. The cause was found to be a misinstalled torque link pin from that mornings tow out of the HAS. The strut extended on takeoff and it became jammed in the nose well keeping the nose gear from extending.
|
|
| 13 Jan 1995 |
[w/o] |
90849 |
90-0849 |
22 FS |
F-16D Block 50B |
|
Details
|
|
|
|
|
Crashed near Durbuy (impacted in a sand trap on the Five Nations Golf Course), Belgium while on a routine training mission from Spangdahlem. The two man crew ejected safely. Backseater was an inlisted on an incentive ride. The crashed caused the grounding of all F110-GE-129 powered block 50 aircraft on the fourth day after, January 17th. A three hour inspection of the fan blades on each aircraft were performed. Some aircraft were flyable the same day, while others over the next few days. This mishap was the third in a row in five months.
|
|
| 26 Jan 1995 |
[w/o] |
89036 |
89-2036 |
510 FS |
F-16C Block 40E |
News Article
|
Details
|
|
|
|
|
Flew into the waters of the Adriatic Sea about 60 miles east of Camacchio, Italy at 08:40 killing the pilot Captain Mark 'Mac' P. McCarthy.
|
|
| 05 Feb 1995 |
[w/o] |
89000 |
89-2000 |
188 FS |
F-16C Block 40E |
|
Details
|
|
|
|
|
Crashed 70 miles southeast of Albuquerque, New Mexico. The aircraft suffered an aft retainer coming apart from the engine. The pilot was Lt Mike Holzer and he ejected safely. Some reports say pilot was Major "Beak" Hulsman.
|
|
| 10 Feb 1995 |
[act] |
83185 |
83-1185 |
309 FS |
F-16D Block 25B |
|
Details
|
|
|
|
|
Collided with F-16C (88-0478) at Luke AFB, Arizona. Aircraft only lost its nosecone and was repaired.
|
|
| 10 Feb 1995 |
[w/o] |
88478 |
88-0478 |
308 FS |
F-16C Block 42C |
|
Details
|
|
|
|
|
Collided with F-16D (83-1185) over Luke AFB, Arizona. Wreckage from the F-16 came down near the runway and within 300 feet of five F-15E's each loaded with four live Mk84's. SSgt. Owens and his crew rushed to unload the ordanance and safety the aircraft. The pilot, First Lieutenant Charles Durfree, ejected safely but broke both heels due to ejecting at such a low altitude with the parachute probably not opening entirely. Captains Barry Beckner and Ben Culp were flying the other aircraft and landed it safely. The other aircraft, was repaired and returned to active duty at Luke.
|
|
| 15 May 1995 |
[w/o] |
78093 |
78-0093 |
148 FS |
F-16B Block 1 |
|
Details
|
|
|
|
|
Crashed at about 14:00 hours in an open range area about 25 miles east of Lordsburg, New Mexico, on a training mission from its base at Tucson IAP. Both the instructor pilot, Lieutenant Colonel Carl J. Thomae and his student pilot, First Lieutenant Abdulla Al-Khalifa from Bahrain, ejected safely.
|
|
| 02 Jun 1995 |
[w/o] |
89032 |
89-2032 |
555 FS |
F-16C Block 40E |
|
Details
|
|
|
|
|
Captain Scott O’Grady’s aircraft. While patrolling the no-fly zone over Bosnia, the aircraft was hit by an SA-6 Gainful SAM. The aircraft came down near the town of Banja Luka, Bosnia. Scott O’Grady was able to safely eject. However, O’Grady spent six days on the ground in enemy territory before being rescued by a Marine Corps CH-53 and support aircraft. Scott was picked up from near the town of Mrkonjic Grad. Scott O’Grady’s story made headlines around the world, becoming a celebrity. He is one of the more well known F-16 pilots.
|
|
| 25 Jun 1995 |
[w/o] |
87273 |
87-0273 |
176 FS |
F-16C Block 30H |
|
Details
|
|
|
|
|
Went down 2 miles southeast of Strum, Wisconsin after engine began to lose thrust. Pilot ejected safely before aircraft impacted the terrain. The F-16 belonged to the Wisconsin ANG at the time of the crash. Some sources have this aircraft lost on June 27, but this is incorrect.
|
|
| 21 Jul 1995 |
[w/o] |
82018 |
82-1018 |
184 FS |
F-16A Block 15P |
|
Details
|
|
|
|
|
The air plane crashed at Fort Smith MAP, Arkansas with the pilot ejecting safely
|
|
| 21 Aug 1995 |
[w/o] |
88455 |
88-0455 |
308 FS |
F-16C Block 42C |
|
Details
|
|
|
|
|
Crashed 100 miles northwest of Luke AFB near Prescott, Arizona. The pilot, Captain Nathan Hill, ejected safely from his aircraft which was on a routine training mission.
|
|
| 28 Nov 1995 |
[w/o] |
88426 |
88-0426 |
4 FS |
F-16C Block 40B |
|
Details
|
|
|
|
|
Crashed near the Dugway Providing Grounds, some 130 miles southwest of Hill AFB, Utah. The pilot, Captain Christopher Rappa, who was on a training mission ejected safely. The aircraft had just been transfered to the 4th FS from the 421st FS a few weeks earlier and new paint scheme applied. Cause of crash was simply a stall at 14,000 feet and aircraft pancaked onto the ground upside down. With no forward volocity at the time of impact, the crash site was little larger then the F-16 itself.
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