| Date |
Status |
Local S/N |
Aircraft |
AF/Unit |
Version |
Info |
Details |
| 12 Jun 2001 |
[w/o] |
89063 |
89-2063
|
USAF 35 FS |
F-16C
Block 40F
|
News Article
|
Details
|
|
|
|
|
Lost forty miles southeast of Kunsan AB, Korea taking the life of pilot, First Lieutenant Randolph E. Murff. It is speculated the aircraft struck an electrical pole before impacting a rice paddy. Cause was later determined to be due to spatial disorientation. The aircraft ended up in an inverted steep dive that was not recoverable (13,000 feet, 460 knots, 59° nose low, 165° left bank). The pilot ejected out of the envelope (one second before impact).
|
|
| 23 Mar 1998 |
[act] |
89067 |
89-2067
|
USAF 4 FS |
F-16C
Block 40F
|
News Article
|
Details
|
|
|
|
|
Veered off Hill AFB’s runway returning from a night surface attack at 20:20 hours. The pilot ejected with minor injuries. Cause of the crash was pilot error. On his approach for landing he failed to use proper decent control due to a step late left turn to line up with the runway. The hard landing resulted in the collapse of the port undercarriage. Sparks and leaking fuel made part of the aircraft to burnout.
|
|
| 18 May 1993 |
[w/o] |
89069 |
89-2069
|
USAF 18 FS |
F-16C
Block 40F
|
|
Details
|
|
|
|
|
Crashed near Eielson AFB, Alaska killing the pilot Capt. Luis F. Jordan during ACM with a British Tornado.
|
|
| 18 Dec 2002 |
[act] |
89072 |
89-2072
|
USAF 4 FS |
F-16C
Block 40F
|
AIB Report
|
Details
|
|
|
|
|
Mid-air collission with F-16C (88-0457). Both aircraft and their pilots returned safely to Hill AB. There was $ 1.7 million worth of damage to both aircraft.
|
|
| 20 Jan 1996 |
[w/o] |
89079 |
89-2079
|
USAF 112 FS |
F-16C
Block 42F
|
|
Details
|
|
|
|
|
Crashed about 10 miles from Cannon AFB at Clovia, New Mexico while on route to Luke AFB, Arizona. The pilot, Col. Phil Lehman, ejected but suffered serious back injuries.
|
|
| 09 Sep 2003 |
[w/o] |
89084 |
89-2084
|
USAF 35 FS |
F-16C
Block 40F
|
News Article
|
Details
|
|
|
|
|
Crashed in the Yellow Sea near Kunsan AFB, South Korea. The pilot, capt. Kevin Dydyk, ejected and was rescued 90 minutes after the crash. Cause was determined as poor situational awareness of a low-altitude condition.
|
|
| 12 Oct 2000 |
[w/o] |
89088 |
89-2088
|
USAF 125 FS |
F-16C
Block 42F
|
News Article
|
Details
|
|
|
|
|
Pilot ejected with minor injuries and the F-16 fell into a field near Atlanta, Kansas. Cause was found to be engine failure after one of the bearings assemblies failed. The engine shut down, causing the pilot to attempt a restart. After the wingman saw fire coming out of the engine, he called for him to eject.
|
|
| 16 Dec 1991 |
[w/o] |
89089 |
89-2089
|
USAF 363 TFW |
F-16C
Block 42F
|
|
Details
|
|
|
|
| 23 Dec 1993 |
[act] |
89091 |
89-2091
|
USAF 112 FS |
F-16C
Block 42F
|
|
Details
|
|
|
|
|
The right main landing gear failed. This caused the aircraft to skid across runway, two taxi ways and the ramp coming to rest in front of the port authority fire department building. There were no injuries.
|
|
| 31 Jul 1996 |
[w/o] |
89093 |
89-2093
|
USAF 68 FS |
F-16C
Block 40F
|
|
Details
|
|
|
|
|
Suffered a Class A mishap, but is surprisingly considered repairable, but most likely will not be repaired. It was written-off at Kirtland AFB, New Mexico. The aircraft was the 3rd out of a 4-ship to take off, but it had no rotation of the stabs and subsequently the nose did not rise. The runway barrier did not raise in time and the aircraft went off the runway. The pilot ejected safely. Pilot had not taken into account Kirtland's high altitude and tried to rotate for take-off too early. There was suspicions of under-serviced nose strut contributing to crash but this was disputed due to the fact that the aircraft still should have rotated and numerous other Moody aircraft had improperly serviced struts and why didn't they have the same problems.
|
|
| 16 Feb 2000 |
[w/o] |
89094 |
89-2094
|
USAF 63 FS |
F-16C
Block 42F
|
News Article
|
Details
|
|
|
|
|
Major Anthony Barrell had problems with his aircraft so diverted to Gila Bend, but did not make it. He ejected at about 12:10 hours. All Luke F-16's were grounded as a result.
|
|
| 21 Apr 1997 |
[w/o] |
89095 |
89-2095
|
USAF 68 FS |
F-16C
Block 40F
|
News Article
|
Details
|
|
|
|
|
Crashed as the result of an engine flameout at a low altitude. The air plane crashed in the southern portion of Georgia, seven miles southwest of Pearson. A malfunction in the main engine control component caused the flame-out. Aircraft was nicknamed Satan and spent a lot of time code 3. The pilot ejected safely.
|
|
| 14 Mar 2006 |
[w/o] |
89099 |
89-2099
|
USAF 35 FS |
F-16C
Block 40F
|
News Article
|
Details
|
|
|
|
|
Lost at sea around 09:30 hours twenty miles off the coast of Kunsan AB, Korea. Pilot was Capt. Donald Siegmund, of the 35th Fighter Squadron ejected safely and returned to base shortly after. He spent about 55 minutes in the water before a South Korean air force rescue helicopter dispatched to the scene found and lifted him to safety.
|
|
| 23 Aug 1996 |
[w/o] |
89101 |
89-2101
|
USAF 34 FS |
F-16C
Block 40F
|
|
Details
|
|
|
|
|
Crashed near Dhahran, Saudi Arabia. The crash was caused by an engine flame-out during take-off. The pilot ejected safely.
|
|
| 24 Mar 2009 |
[act] |
89102 |
89-2102
|
USAF 510 FS |
F-16C
Block 40F
|
News Article
|
Details
|
|
|
|
|
Suffered an in-flight emergency which led to the pilot deciding to drop the external tanks which landed in a local village. The aircraft landed safely at Aviano AB.
|
|